Delayed fracture occurred to a temporary anchor supporting an overhead powerline during construction. The fracture resulted
in loss of the overhead transmission line and resulted in a singe vehicle incident in the adjacent roadway. Post-failure analysis
conducted as part of personal injury litigation revealed that the fracture was precipitated by a pre-existing weld related
crack. Closed form and numerical stress analyses were conducted in order to assess the role of anchor installation in the
failure, with the results indicating that installation was not conducted outside of the parameters intended by the anchor
manufacturer.
Keywords Weld related cracking - Delayed failure - Residual stress